5/14/12
I made a discovery this weekend about which I am not too pleased. Juan may remember that I had a theory as to
why George “overheated” when we fired it up.
Said theory being that with the heater capped off there was not any
water flowing out of the back of the cylinder head to “burp” it properly. Yeah, the heater is not capped off on
George. In fact, it actually has an
extra “circuit,” if you will, teed off of the heater to send water to the
turbo’s bearing section. I am at a loss
now as to why the thing got hot. I guess
I should say I am AGAIN at a loss as to why it got hot. I am back to a fear that the cylinder walls
might be too thin. I haven’t mentioned
this to John because… well, I guess I just didn’t get around to it. I fingered, I guess, we would “discover” it
together when we brought the car back in to finish it. So why am I bringing it up now? Well, because it is 0900 h Monday morning and
I'm already bored with work. I'm afeared
this is going to be a LONG week… made longer by the fact that John might not be
able to come to the shop on Saturday.
Sure, we’re “planning” to go on Sunday instead, but I'm not holding my
breath. Anyhoo, we’ll see how all that pans
out. As for this last weekend, here’s
what went down. I got up at my usual
0530 h to feed the cat. I think I might
have tried to go back to bed for a bit but gave up pretty quickly. I dressed and went to the shop arriving at
around 0730 h. I had the new Saiga,
Woody, with me along with all the parts I was going to install: the trigger
group, pin retention plate, and safety.
The recoil buffers I ordered hadn’t arrived but I knew I could install
them at home. I disassembled the weapon
and cut the trigger off of the sear in the new trigger group. I was in the process of fitting the trigger
group when John arrived. Since the new
hammer was not trimmed for the Saiga’s bolt hold open, which is a total pain in
the ass to install anyway, and the safety has a BHO notch cut in it, I discarded
the factory BHO and its spring. Ok, I
didn’t discard it, but I didn’t install it either. With the new hammer, trigger group, and plate
in place, I tried out the action. Oh
yeah, that’s one nice trigger now.
Before it was almost awful, now it is very nice. You just have to feel it to know the
difference. Anyhoo, I reassembled the
gun and put it away. Meanwhile, John
painted the area under the grille, and the grille, of Lil' Wiggly. It looks so much better. I made the linkage for the carburetors even
though the lever arm still hadn’t arrived from Italy. We piddled around until about noon and went
for sushi… sort of. We didn’t have any
Nigiri, which is the bit of bait on a blob of rice which most people think of
when Juan mentions sushi. No, all we had
were rolls, which are still technically sushi, so I'm going to hang my hat on
that. We ate way too much. Eventually we parted ways and I went to
O’Reilley’s to look for a master kill switch and a momentary off push
button. I found the kill switch. I bought it and a 12” black battery cable
with rings on both ends. Back at the
shop I had a look at installing it. My
first thought was to make an “L” bracket to mount it to a vertical surface
under the hood. I couldn’t find any
suitable metal. Next I thought a flat
bracket could be used to come straight off of the relay box next to the
battery. Again I didn’t find any metal I
liked for the job… not to mention I could only find one nut and bolt
combination which would fit the thing.
Then I noticed a flange sort of thing on the side of the radiator where
Juan is supposed to mount the fan shroud.
I did a test fit of the switch and found it would fit nicely there. I bolted the two battery cables to the switch
and the switch to the radiator. I hooked
up the cables to their respective locations, chassis ground and battery, and
gave the switch a test. Of course it
worked. Next I moved on to filling the
hole in the dash where the wiper switch used to reside. I found a panel clip thingy from one of the
Versæ and tried it in the hole. It was too
small to fill it. I took a vacuum plug
and stuck it on the clip and tried to insert that in the hole. Now it was too big to fit. I took the vacuum plug and stuck it on the
clip from the back side of the dash and now the hole is filled. It is a bit ghetto but I'm going to go with
it for the time being. Marty Smith
showed up so I showed him a thing or two we had been working on since his last
visit. While showing him the headlights,
the fuse blew. I replaced it and the
headlights worked again. Eventually we
both left and I went home. Sunday I met
mom at church then took her to lunch. I
thought about taking The Seven to get an inspection but decided I'd do it next
Saturday at my usual place. Besides, I
need to change the oil and might as well do that while I'm alone at the
shop. So, I guess that’s about all I
have for y'all today. Smell ya later.

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