1/28/13
John finally showed me the hydraulic parking brake thingy he’s been gassing on
about. I guess it will be acceptable
after all. I'll order one this Friday
after I get paid. I mentioned last week
that he has ordered an Etcetera master cylinder and the requisite brake pads
for Lil' Wiggly. Apparently one set of
pads are already at his house and I'll bet the others arrive today. The master cylinder might not come until tomorrow
but even if it doesn’t arrive until Friday, we’ll still have it for next
Saturday. As for what we achieved this
last weekend, well the 302 is just about completely dressed out. We have fingered out how we’re going to route
the serpentine belt as well. What we did
was take an “inside” idler and moved it up to a position which used to be an
“outside” idler. This now gives us a
nice belt route which otter work… if we can find a belt in the right
length. We also need an alternator but
John has an e-mail out to a dude selling some on e-Bay. Said dude has a 1.21 gigawatt unit for Fjords
as well as “one wire” units for… um, other things I guess. John has asked if the shell we need can have
the self-exciting thingamajigs installed in it.
I'm trying my best to not be “That Guy” by sending John an e-mail asking
if he’s heard anything. He’ll let me
know when he hears something. Anyhoo, we
installed the chrome valve covers on the engine and decided to go ahead and run
a PCV valve for a myriad of reasons. Of
course, the environment was NOT one of them.
Sucking down the crankcase does make a wee bit more power and helps to
reduce oil consumption, but the main reason was the valve covers have the
grommet holes at the front on one head and the back on the other. We put the cap to the front and the PCV to
the back. I stole the PCV valve and hose
from the A-14 we took out of Lil' Wiggly and it plumbed right up to the
carburetor… but I'm getting ahead of the story.
Once the valve covers were on, I had a look at installing the intake
manifold. I cleaned up the surface and
pookied around the ports before plopping the gaskets in place. A wee bit more pookie around the ports on the
manifold side and I declared, “Note to self: ‘Make John scrape the gaskets if
we have to change manifolds since the pookie was his idea.’” He laughed… I think. We then discussed the merit of blocking off
the exhaust heat riser passage between the heads under the carburetor. It was decided that a piece of Dr. Pepper can
pookied over the holes should do the job.
This I did. I'm beginning to wish
I'd put the bits of can on the head side of the gasket rather than the intake
side and I hope to hell we don’t blow through the gasket into the intake tract
or lifter valley. I didn’t realize my
mistake until it was way too late though… like last night in bed. Oh well.
I installed the intake and hunkered down on the bolts. It looks so good! I installed the studs for the carburetor and
greased up a gasket for it. With the
carburetor on and bolted down, we had a look at the 14” air filter which came
with the kit. It looks nice… but it
won't clear the HEI distributor. We had
a look at that velocity stack air cleaner I made for Mr. Wiggly but it just
would not fit any more. I will order a
10” filter from Summit soon. We dropped
the HEI dizzy in and John took some pictures for the build thread. It was at this point that we actually began
looking at the belt situation. I bolted
the alternator and tensioner bracket back on the engine and looked to see if
there was any route which would work.
There wasn’t. I bolted the A/C
and power steering bracket on as well and had a look. If we swapped the “inside” idler from the
A&T bracket over to where there is currently an “outside” idler on the
A/C&PS bracket, we would have a good route.
As I mentioned before, this is what we did. We marked what could be cut off the
A/C&PS bracket and John took it to the vice. I'll probably take the Saw-saw to it next
weekend. We may or may not “add
lightness” to the A&T bracket but what there is to cut off isn’t very
much. It may just hang there as
superfluous material. We’ll see. I think that was about all we got done on my
engine. John did some stuff with his
engine and I believe it is ready to bolt into his car. He just needs to finish up his steering
conversion before we can do that. We
went to have sushi and then both called it a day. I didn’t go back to the shop because my
brother was supposed to come to the house at noon and she had some church thing
she wanted me to go to with her in the evening.
I did stop by Sutherland’s Hardware to look for a 1/8” female to ¼” male
NPT adapter thingy, preferably a 45°, for the oil pressure sending unit on my
engine. They didn’t have one. I got home apparently five minutes after my
brother left. Oops, shouldn’t have
stopped at the hardware store. I cleaned
up and took a nap with the cat. Mom wake
me up to say she was going to the store and that she wasn’t sure she wanted to
go to the church thing after all. I put
up no argument whatsoever to that plan.
We did skip it, much to my relief.
Ok, as usual I think I'll save Sunday’s tale for tomorrow. Have a day.

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