2/25/15
Well, I would have gone to the shop to install the
voltage regulator on Scooby Two Saturday but it wouldn’t start. I could have jumped it off but for some
reason just didn’t. With winter weather
forecast for Sunday I decided that I would do it after lunch. Yeah, it was raining after lunch so I
didn’t. That was either a big mistake or
just a, “Meh, whatayagonnado?” Monday
morning it was icy… like “Hmm, I can’t get out of the driveway today,”
icy. I gave passing thought to trying to
jump-start Scooby Two but blew it off and hopped in Fiona. I tried to go to work but I literally could
not get Fiona up the hill in front of the house. Hell, it was all I could do to get it back up
the driveway to re-park! In fact, the
car sat half the day all catty-whompus in the middle of the drive. Eventually, when I gave it one more attempt
to go to work around 1100h, I got the car parked properly… after not being able
to get up the hill again. By 1500h I
decided that I wasn’t going anywhere and changed into comfy clothes and settled
in for some marathon “How It’s Made” on the Science Channel. Oh, and I napped a lot. Tuesday morning wasn’t too bad. I got up early again and was able to get out
of the neighborhood finally. The roads
were not bad but I didn’t take any chances.
I ran both stop signs at Chapin road but got stopped by the traffic
light at Hwy 80… or what the hell ever they are calling that fucking road
today. I mean seriously, they change the
name of that fucking spur of asphalt more often than I change my mind on Datsun
stuff! But I digress. Once up onto the freeway it was smooth sail…
WHOA! TANK SLAPPER! I was doing about 40 in 4th gear,
keeping it nice and smooth, running true when the ass-end started to step
out. A few degrees of counter-steer and
the car shifted into the center lane.
Fortunately no one was next to me.
The tires bit on clear pavement and straightened out… for about a
quarter mile when it stepped out again.
More counter-steer and it caught again.
After those two sphincter-flexers, I kept it at 40 but went up to 5th
gear to reduce the torque at the wheels.
The rest of the drive was uneventful.
Going home was pretty normal.
This morning I was expecting snow on the ground… it was raining. As soon as I walked out the front door
however, it started to sleet. “Are you
fucking kidding me?” I yelled at the sky.
I got no reply except for more sleet.
By the time I got to work the sleet turned into snow. Now, I hesitate to call those things “flakes”
because they were more like… well, I don’t know exactly what they were
like. All I know is they were so big
that I could feel them hitting me through the leather jacket! We got a little accumulation but by 1030h the
sun was out and it was looking like nothing had ever happened. So, the whole reason for me having Scooby
Two, besides it being given to me, was to spare Fiona from wintry weather
driving… and it failed that task miserably.
(Slow clap) Way to go Scooby Two, way to go. So, there’s THAT going on. Oh, I just remembered why I didn’t work on
Scooby Two Saturday afternoon. I decided
to take the Saiga 12 to the range to burn up some ammo and make sure it was
reliable. I waited in line for a bit and
was finally allowed into the range. I
loaded up all four 5-round magazines and the 8-round mag. I sent a target out and racked one into the
chamber. Line up the sights, squeeze the
trigger and… nothing. Damn that
safety! I flicked off the safety and
tried again. BOOM! Flutter, flutter (that’s the target by the
way). “Nice,” I thought, and lined up
the sights for another shot. Squeeze the
trigger and… nothing. “Ok,” I said to
myself, “it ain’t the safety this time!”
I dropped the magazine and racked the action. Sure enough, it hadn’t even tried to eject
the spent shell. I was just about to get
pissed off when I remembered that I have an adjustable gas plug and that it was
set on the absolute minimum level. I
adjusted it out one click and reloaded.
BOOM! Flutter, flutter. I smiled and went for a third shot. Ok, I’m not going to go for the drama this
time. It didn’t cycle again. I opened the gas system up one more click and
tried again. BOOM! Flutter, flutter. BOOM!
Flutter flutter. “AW HELLS YEAH!”
I said to myself. I emptied the rest of
the magazines and decided that I’d had enough.
I’m happy with the way the gun runs buckshot. I stopped at Academy and bought fifty rounds
of ammo to replace the 28 I’d shot and then went home to clean the gun. Then, in a monumental case of dumbassery, I
started looking at accessories for the Tavor online. I found a neat little rail system for it and
was just about to not buy it when I watched a video about it. Apparently with this rail system, you don’t
need to remove it or the optics to remove the barrel from the gun. I’d really like to be able to clean this
thing better so I was sold. I ordered
it… and the little tool for removing the barrel… and four more 40-round
magazines for it. The magazines are for…
well, you see it’s like this… I have a compulsion to fill empty pockets. There are five magazine pockets on the
outside of the range bag for the Tavor.
I couldn’t let them sit empty. I
filled the pockets on the Saiga 12’s bag with magazines, I must fill this bag’s
pockets. I must… seriously, I MUST! Anyhoo, I had a look at the one 40-round
magazine I already had and it fits perfectly… so I bought four more. Bah!
Like I need to ‘splain myself to you!
Well, now the folks at work are asking me to do… work, so I guess I’ll
go do that. Have a day.

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